Well today was the day to fit the rear axle & get it back on its wheels. Did we suceed in doing that?? errr.......no.
We had a lot of fun getting the diff on the trolley jack & manouvering it under the car. It was nice and stable as I had cut a wood board for it to sit on so it was no problem to roll it into position.............where it promptly decided it was nose heavy and fell off the jack
No harm to the diff but a bit of a chunk out of the concrete floor
It was a bit of a challenge for us both to lie under the car & lift it back on but we prevailed.
We then bolted it back in place to the crossmember - made quite difficult as we had already installed the fuel tank which restricted access but we succeeded in the end. I then wired the bolts up and fitted the handbrake cable while Phil sanded the other door for polishing.
When it came to fitting the cable to the actual handbrake I had to look for the clip in the tin of parts.........where I realised the nipple on the cable would pass through the hole in the clip. Now what was needed was some kind of ferrule on the cable to stop this..................probably the sort of thing that might just have been on the cable the day before that I thought was surplus to requirements and had ground off with the angle grinder.........
So I had to make a new one out of a drilled and countersunk bolt with a groove cut into it, the nut secures it nicely to the clamp and also prevents the cable coming out. Unfortunately this is a little thicker than the original fixing so the cable seems to be slightly short which results in the brakes being on with the handbrake in the off position. So tomorrow I will make a new clip to link the two that will be a little longer to give us some free play.
We then went on to fitting the new roller bearings into the second fulcrum arm. The first set went ok, but the second set fought us all the way. Once installed the bearings clamped almost solid on the bearing shaft sleeve. So...out they came for inspection and we tried a different bearing and installed them with the bearing shaft sleeve in the bearings to make sure they were parallel when being fitted.
Still too tight for my liking
We repeated the fitting & removal several times and in the end I resorted to sanding the inside of the fulcrum arm bearing holes with some 280 grit paper wrapped around a long socket to remove a few thou of metal.
After a bit of messing around we got one bearing with nice tolerances but the second one was still wrong. I fished out the last 'spare' used bearing - it was the least good one so it was the last resort, but when it was fitted it was within tolerance with smooth turning and the inner shaft was a good sliding fit with no more binding so we called that a win.
Then we discovered the joys of trying to fit the fulcrum arm back on the diff
Not very easy when the gap between the arm with the seals & washers fitted was 1mm smaller than the width of the axle bracket. So, the nice shiny paint was filed back off the mating surfaces on the diff and we tried again.....and again.....and again......
Eventually we succeeded using a big screwdriver as a lever to create enough of a gap that we could gently hammer the seal & washers in with a rubber mallet.
All of this used up a large amount of time as these things do, so we mocked up a hub carrier and loosely fitted the shocks just for the fun factor. Hopefully tomorrow the other side will go a lot easier! The plan is to get it back on it's tyres again by the end of the weekend.
I can't really tell, but Phil could see the difference of the narrowed axle. With a quick bit of checking the wheel backspacing and some eyeballing from above it looks like I got all the measurements correct and the tyre should just be a finger width inside the arch. Phew!!
852.75 hours.